Foam, dust, spars and sails
At the students’ behest (honestly, it doesn’t take much arm twisting) we spent a class period in the shop and managed to make significant progress. I’d done my best to line up some projects and materials to maximize our time, and I was eager to capitalize on their enthusiasm.
Kaitlyn and Klara went right to work on cleaning the spars with 3M’s restorer compound and wax, while Simone and Becky sanded the cockpit seats. Michael R., Jared C., Tony, and Michael H. sanded the cockpit slats, which we’d disassembled yesterday evening, and the cockpit coaming. A few of them have a study hall following our time together, so they stayed on to continue working and managed to get the wood completely sanded.
Michael D. and Joey did their best to remove the remaining forward attachment for the rub rail and loosened the stem fitting before making a supply run. I drilled out a rusted fastener to complete the rub rail removal, and pulled the last bolt to free the stem fitting. Both the rub rail and stem fitting need attention. The forward hole on the stem fitting is cracked, and the rub rail could use a good cleaning. Both should be repairable. I tried cleaning a small portion of the rub rail to see what it would look like, and I’m satisfied that it will clean up just fine.
Bonnie and Alex G. filled a tub in another room and began cleaning the mainsail. It is in fair condition, but has a few stains from rodents (not to mention a smell) that we’d like to get rid of – or at least improve. The sail should be serviceable.
Matt and Matt got some kerosene and began cleaning up our bucket-o-parts: winches, cleats, chainplates, and other hardware.
Constanza and Josh did their best to dig the pour-in expanding foam out of a small cutout in the lazarette. I don’t think they made much progress thanks to the small opening. It appears it’s going to be necessary to open that hole up if we’re going to get the foam out. And the foam must be removed if it’s as bad as what we found in the cabin.
Nick, Alex and I worked on demoing the cabin. Armed with a Sawzall, we cut away the v-berth to expose the foam, which had collected so much water that it spurted out of the cuts and flooded the sole. Every piece of plywood and every section of foam was saturated. We carved out shoebox-sized chunks of foam, each one weighing a couple of pounds. The task was made more enjoyable by the discovery of colonies of black ants that had been happily munching on the rotten wood until we disturbed their tranquility. Little by little we hacked away at the water-soaked foam, stopping periodically to shovel it out of the way.
After we’d cleared the cabin, we cut through the forward bulkhead. Again, water poured from the cut. I had estimated earlier that the forepeak and v-berth probably held close to 200lbs of water. I’m pretty certain of that now. We hauled several loads of foam to the dumpster, each weighing 40lbs or so.
We found a shovel to be most effective, if not a bit unwieldy, at carving out chunks of foam as we excavated the forepeak. The Sawzall was useful at times, but the shovel enabled us to pry large chunks free fairly easily. Nick and I worked until 5:30 before calling it a day.
Things are moving right along.